CRUSTY QUINNS
TECH TIPS
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Stator.
Posted by JAW Note: This is an update of this page due to many questions asked
about how well it worked.
The XR has always been very hard to start. At first people would say "heh, yeah, those
single pot 600's are buggers to start." When JAW was starting to walk around in circles
because his right leg was twice as big as his left leg, he began suspecting carby
troubles. "It only starts when it has the exactly the right amount of fuel in the pot it
seems. Too rich, it wont start. To lean, it won't start."
Finally Wise Wolfie said "JAW check your spark." "Yeah, it sparks Wolfie, it wouldn't
run at all if it didn't spark!" "Humour me."

Stator in the rotor cover.
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Weak spark?
Behold and lo, the was the wimpiest pale spark you've ever seen; it would have
battled to fight it's way out of a wet paper bag. That kinda makes sense - a fat
spark would ignite fuel in up to the worst conditions, but a wimpy spark would need
"perfect" conditions to get the show on the road. Well that's what JAW thought
anyhow.
So what does a weak spark mean? If you look at a bike sparking system there is
the spark plug, the ignition coil, high tension lead, wiring, the pulse sensor, the
CDI and the stator exciter winding to generate the power.
The problem was isolated using another bike to swap and test parts - it had to
be either the CDI or the exciter winding. But do you think you can get a motorbike
shop to test a CDI? "Hey guys, have you got an XR600RJ that you can verify the
operation of this CDI on?" "Oh, no no no, you must go and pay $'00 to the Master
Motorbike Electricals Guru, it's all magic, only he knows how it works. Blah blah
blah.
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Gotta be the exciter winding...
JAW makes a bold decision: "CDIs are electronics. They either work, or they
don't work. I reckon that tiny, thin winding of enamel wire that is subject to
heat, oil and works from a permanent magnet is *far* more likely to be the
problem.
Before you go any further, I want to know how it all works.
Okay! Firstly, there are two separate circuits on the average bike - a low
voltage power source for running accesories such as headlights and indicators, and
a high voltage power source (known as the exciter winding) for getting the CDI to
spark. 'Crossers might only have an exciter winding - what's a headlight anyway?
;)
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Exciter winding at the top. 2x2 Lighting windings either side.
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Winding notes...
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Now the rotor, the thing that spins around the stator, is magnetic. It has
several poles, you know, Norths and Souths, on it. On this particular bike there
are 6 Norths and 6 Souths. As the rotor spins around the exciter winding, thanks to
some rather convenient physics current will flow in the winding. As a North pole
passes, current goes up, North then swings back to neutral (ie no magnetism)
current goes to zero, South pole passed, current goes the other way. Yep, it's AC
(Alternating Current).
The more windings you have the higher the voltage. By winding the exciter with
*heaps* of turn with really thin wire you get high voltage, low current. Using
thicker wire, less turns, lower voltage, higher current.
They got clever on the lighting side of things. The four windings are just one
piece of wire, but it is wound clockwise on the first pole, anticlockwise on the
second pole, and so on. Why? They are positioned so exactly as a North pole is
going past the first winding a South pole is going past the next winding. What does
that give you? Well, the current flows depending on which way the winding was
turned. So, in effect, by having the opposite pole and the opposite winding
direction, the currents all add up. If you didn't alternate the winding directions,
the currents would actually cancel out...
The advantage is of course that you get quadruple the output - each individual
winding is good for around 3V but 4 of them gives your 12V. Note that the actual
voltage is dependent on rpm but then controlled by a regulator to maintain 12V and
then rectified where necessary, but that's another story.
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The empty pole, ready to receive some wire. My, the right most lighting pole
is looking a little black isn't it?...
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Rewinding, a process.
On with the story. Specifications for an XR600 between 1985 and 1990 state that
the exciter to ground resistance should be between 230 and 320 Ohms. My old one
came in at 370.
Ripping off the old winding revealed the problem. Enamel had been baked black -
but there were no short circuits. The wire in places was so incredibly thin and
just broke apart as it came off. What must happen is the copper itself is getting
old and sad, its resistance increases and it's ability to carry a current
diminished. Hard to start but will run okay.
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You'll need to find yourself a big spool of hair-thin enamel winding wire. I
came across this one from the olde man in laws shed. It's 0.132mm, vintage 1978 and
all...it's fatter slightly than the existing windings, so to replace the same
number of turns it will be a physically bigger widning. Oh well.
Try and get good quality winding wire with the highest temperature rating on it
as possible. Inside the engine can get really hot being aircooled - much hotter
than a water cooled engine.
Set yourself up so the wire can freely pull off the spool and just wrap, wrap,
wrap. It's suprisingly strong for hair-thin wire but don't take any chances. Do a
few stress tests on it before you begin, see how easy/hard it is to snap it . You
want one winding, you don't really want any joins.
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Set yourself up first, you want to be able to drag wire off the spool
easily.
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Halfway - careful does it!
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After about an hour, yeah, just an hour, it was wound to where I thought it
should do. A fair bit bigger than the old coil. But how do you know when to stop?
Carefully peel off a bit of enamel and do a resistance check. I found a sharp knife
scraping both ends enough for a connection would do the job. First check - 162
Ohms. Keep going. Second check, 250 Ohms. That will do.
Carefully solder on some flyleads and expoxy the thing in place to protect those
precious little windings. I used some devcon I had lying around, it isn't
conductive, it is tough as, it seemed to do the job.
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Results
Okay, the winding was a success. The bike started nice and easy which was a
pleasant suprise; but as time went by it got less easy. Until finally, a year
later, out in the bush, it refused to start.
What could have happened?
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Protect your windings.
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14mm deck height max.
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Measuring the resistance back in the shed showed the resistance was still
250Ohms. Kickedy kick, nothing. Retest the resistance down to 150Ohms. Huh? a while
later its at 210Ohms.
Right, its coming out again with two plans: (a) find out what went wrong and fix
it and (b) Rewind the lighting circuit - I need some decent headlights!
First thing I did was check the how big a winding you could put in there
physically. The plasticine test revealled 14mm deck height maximum.
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While degreasing the winding I found out the first problem - water dropped the
resistance right down. Ah ha! Must be an internal short. As I unravelled it the
truth became clear. Oil and heat had broken down the enamel protective coating and
caused intermittent shorts. But how did the oil get in?
I may have epoxied the windings on the outside - but oil found it way past the
exciter plastic spool from the _inside_. The new attempt was firstly going to have
to be plastic spool-less and secondly epoxied all the way! The Devcon epoxy used
proved up to the heat and oil challenge - even though it had changed colour from
gray to dark brown.
With a bare stator in my hand, first thing to do is "dunk" the think in epoxy -
so that the first windings aren't sitting on metal but sitting on a protective
coating of epoxy over the metal. This is how they come from the factory.
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Stripped back and re-epoxied.
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Lighting circuit done.
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I rang around a bit and found that there was such a thing as high-temperature
enamel. Normal enamel winding wire is rated to around 120-130degC. Super-enamel can
go out to maybe 200 but I couldn't source any locally.
I decided to stick with the wire I used last time, but from the moment the first
windings went on I was popsticking on epoxy for a "total seal". Nothing was going
to get in there. This time I wound all the way out to 310Ohms. The winding was
looking pretty oblong since there was no spool to neatly wind onto, but it hasn't
caused a problem so far.
The lighting circuit copped some 0.8mm winding wire worth about $5 from the
local electronics store. I counted 64,66,70,65 turns pulling the old wire off - I
decided to wind on 75 each "since the rotor was old and the magnetism was probably
not as good as it was in 1987".
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While I was there I also replaced the insulated wire out of the rotor case up to the
CDI®ulator. Note that normal wire is no good - find yourself some silicone
insulated wire. Not only will it take up to 200degC but it is also immune to the effects
of oil and other nasties.
So where are we at?
The lighting circuit 75 turns was maybe a bad call. I seems to have blown the
regulator - the voltage and/or power went too high. I put a test 24V 100W globe on the
unregulated winding, the voltage went up to 30V and the globe blew; not even close to
full revs. That will require some thought - current plan is a home made regulator and
perhaps to run the system at 24V instead of 12. That would have the advantage of using
all the available power those extra windings added on - 100W or more instead of the
measly 50 or so the bike came with. It may yet be a good thing.
The exciter winding has worked yet again, big spark, did not kill the CDI. It is
pumping out around 90VAC at idle. Now it's the waiting game - will the enamel take the
heat fully epoxied or will the same thing happen? Only time will tell...
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